INITIAL
DESIGN
The
weather station’s original rain gauge was a
disappointment. It worked for only a season
before it started to give me trouble. When I
opened the enclosure to troubleshoot the problem,
I discovered signs of corrosion. Water had damaged
the circuitry. I guess there was no surprise
there, but it wasn’t something I had anticipated.
The socketed ICs were no longer making connections
in the sockets. This problem seemed easy to
solve. I decided to simply “pot” the circuitry
in epoxy so no water could get at it, just like
they do with automotive modules. Unfortunately,
I couldn’t fix the rain gauge right away, so
I had to use the “manual” rain gauge for a few
years.
During
this time, I started another project involving
liquid levels. I needed to measure the water
level in a cistern. No problem. I simply built
a longer version of the variable capacitance
rain gauge unit. And that’s when I found a problem
with the design that I wasn’t able to solve.
When the variable capacitance sensor was allowed
to remain in the water, its capacitance changed.
Despite
having tried several different sensor configurations
and wire insulations, I couldn’t build a sensor
that would produce a stable liquid level reading
from one day to the next. I ended up abandoning
the variable capacitance sensor for that project
and using an electronically simpler approach
that was mechanically more complicated: a float
with a cable pulley arrangement connected to
a 10-turn potentiometer. It worked great. There
were no stability issues.
By
the time I finished the water level project,
I had come to the conclusion that if I ever
got around to upgrading my weather station,
I wouldn’t use a variable capacitance sensor,
despite its elegance. I’d have to find something
better.
The
station’s weather vane has worked fairly well
since 2000. I’ve had only one minor problem
with it. The magnet that rotates over the reed
switches to activate them fell off the aluminum
disk to which it was epoxied. Apparently, epoxy
doesn’t adhere well to magnets. So, I had to
reattach it with another adhesive. It has stayed
in place ever since.
Eventually,
there will be a problem with the reed switches
because the vane constantly waves back and forth
in the wind. The trees may be too close to my
weather tower. The waving constantly activates
several reed switches and will certainly lead
to switch failure.
The
rain skirt that’s supposed to keep water out
of the top bearing that supports the vane arm
will also cause a problem in the future. It’s
just a thin plastic cup (a plug for a cardboard
mailing tube) that will surely fail in the sun
and rain. It’s still intact, but I’ll have to
replace it if I want the unit to remain in service.
There’s
an aesthetic problem with the weather vane too.
The lower part of the unit is housed in a steel
box that has holes bored into it to allow air
to circulate. The lower box also houses the
relative humidity sensor. So, even though the
box is painted, rust has blossomed from the
holes and it’s extremely unattractive. The lesson
here is to use aluminum because it doesn’t rust.
The
anemometer in the original system has been a
stalwart unit. I initially made a serious mistake
with it, however. In an effort to have it work
in the cold, I took the shields off the bearings
and washed out the grease. After a year or so,
I noticed the bearings were noisy. It turns
out that when there isn’t any grease on the
bearings, they are subject to condensation and
rust.
The
unit has continued to work though. Oil has been
the only lubricant on the badly worn bearings.
This anemometer has the same rain skirt as the
weather vane.